Anyone else ever seen this before? 1.6L 16v Stuck intake valves. Run then lose compression over night. Then run then lose compression 5 hrs later?
I towed my Junk 500 miles round trip to the Zu event and back this weekend.
.......... My 4-dr Kick never ran....
This was the first run for my lifted 4-dr after sitting up for 18 months, while I played with the new Rock buggy. The fuel in the tank had fouled and killed the pump. After installing a new fuel pump the truck fired right up and ran well. I washed it up and loaded it on the trailer for my trip. Apparently the gremlins attacked it full force on Thursday while I was at work and by Friday morning it had mysteriously lost all compression while sitting on the trailer. WTF (Never seen that before) ~ I had just driven it on the trailer with no issue two days before.
Wrenching last minute Friday morning in shear panic I checked the timing belt, cam timing and other obvious stuff. Thinking it was fouled fuel related (Weeping injectors / stuck rings) I oiled the cylinders with marvel mystery oil and magically got it running again with good compression numbers 175 x4 . I then let it run for 2 hrs and shut down / restart Ok. Finished packing and left for the ZU around 2pm.
At Wal-Mart in Troy 200 miles from home and 10 miles from the event. I tried to start the Kick but again no compression. Strange being I just had it running 5 hrs earlier
So I stopped by Advance auto in Troy for more Marvel Mystery oil and some sea foam fuel treatment. Saturday morning I oiled the cylinders and played with it for 2+ hrs before removing the valve cover and finding 5 stuck intake valves. I oiled the valves with Marvel Mystery oil and later with Kroil (Better than WD-40). Then I proceeded to tap them with a hammer and screwdriver ( just a shock vibration to loosen them up). I was able to free up a few and restore compression back to cylinder #1. Eventually I goofed up and knocked a spring retainer clip / keeper loose on #2. I ended up partially dropping an intake valve / releasing a spring. Working to reset it with a rope in the cylinder would hold the valve up but compressing the spring and reseting the clips under the cam was not gonna happen with out removing the cam & maybe the head too.
So while I still had 1/2 of sat left I reassembled, re trailered and focused on spending time with the family around the camp. The Friends Dinner & Camping were great and my family had a good time anyway.
Hopefully I'll get it back up and running again soon.