Howdy all! I have a 11 of 87 sammy with 150K+ on it and it blew a head gasket back in October. It was my daily driver untill then, then I put her in the garage till about two weeks ago. I pulled the head in November, took it to a reputable machine shop, everything good. Bought some parts online from Cali, and another 87 zuki that had been rolled for spare parts. I put everthing back together..in 15 degree temps (garage not heated) everything went together great after a good cleaning, and it ran fairly good, a little doggy but not bad. I drove it around, changed the oil and coolant once more, and thought everything was good. Drove to work (95 miles one way) no problems at all, but the return trip netted me with overheating, checked the coolant, almost one gallon low and down by 3 qts. oil
Plus the return of some white goo on the dipstick, and brown goo in the coolant. Filled everything back up and it stayed cool, no knocking or anything, it even ran a bit better!!!! It's once again my DD, so i'm up in the air on what to do next.....